Difference between revisions of "Minutes-9-22-2011"

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= Minutes =
 
= Minutes =
  
Participants: Eugene, Bill, Dave, Chris, Simon, Beni, Vladimir, Mark, and Lubomir. Vladimir is a new graduate student from MePhi Moscow.   
+
Participants: Eugene, Bill, Dave, Chris, Simon, Beni, Vladimir, Mark, and Lubomir. Vladimir is the new graduate student from MePhi Moscow.   
  
 
== Production ==
 
== Production ==
  
- Dave: started checking the continuity before taking the frame out of the stringing table: on the wire frame for cell#5 (that was just finished) one broken wire was found and was fixed today. Epoxy will cure overnight and tomorrow we will put on the stringing table the wire frame for cell#3 to fix one wire there too. Wire frame for cell#4 is ready, just needs last cleaning. On the last cathode (for the first package) the rigid-flexes were glued to the cathodes. Next, they will be tested with a generator and then the daughter cards glued.  
+
- Dave: started checking the continuity before taking the frame out of the stringing table: on the wire frame for cell#5 (that was just finished) one broken wire was found and was fixed today. Epoxy will cure overnight and tomorrow we will put on the stringing table the wire frame for cell#3 to fix one wire there too. Wire frame for cell#4 is ready, just needs final cleaning. On the last cathode (for the first package) the rigid-flexes were glued to the cathodes. Next, they will be tested with a generator and then the daughter cards glued.  
  
 
- We discussed the reason for these broken wires, so far we had always one broken wire per plane. On the last one found on the frame for cell#5, we looked with a microscope. The wire was broken at the end of the epoxy right where it touches the soldering pad. The wire tip was bent at ~90 deg at this place somehow. It was not clear if the tip was inside or outside of the epoxy. The wire was checked by doing tension measurements on it. The only operation that happened later was cutting the wires and then doing the continuity measurements. One explanation could be a cold solder and then the wire brakes when twisting it. Dave suggested also that if the wire is above the PCB it may not be fully covered with epoxy and is easily breakable a that point.   
 
- We discussed the reason for these broken wires, so far we had always one broken wire per plane. On the last one found on the frame for cell#5, we looked with a microscope. The wire was broken at the end of the epoxy right where it touches the soldering pad. The wire tip was bent at ~90 deg at this place somehow. It was not clear if the tip was inside or outside of the epoxy. The wire was checked by doing tension measurements on it. The only operation that happened later was cutting the wires and then doing the continuity measurements. One explanation could be a cold solder and then the wire brakes when twisting it. Dave suggested also that if the wire is above the PCB it may not be fully covered with epoxy and is easily breakable a that point.   
 
   
 
   
 
- End of last week we put three cells in the package after replacing two wires in the second cell and changing all the O-rings.
 
- End of last week we put three cells in the package after replacing two wires in the second cell and changing all the O-rings.
The first three cells were tested channel by channel by Vladimir. All were OK except no signal on one wire channel in the new third cell, most likely broken wire. We found again gas leakage in about the same area as with the two cells. The amount of leakage was about the same (bubbling above 80-100 ccpm) as with the two cells, indicating that the problem is in the second cell. Bill suspects it is the seam on the wire frame between the PCBs that may have been somehow damaged during the installation. To fix the broken wire and look at the leakage place we decided to unstacked the package down to the second wire frame. After finding the broken wire on the frame that is on the stringing table we decided to continue with this tomorrow.  
+
The first three cells were tested channel by channel by Vladimir. All were OK except no signal on one wire channel in the new third cell, most likely broken wire. The third cell was conditioned with HV relatively fast, but then suddenly developed very high current; we left it over the night at 1kV and then in the morning it was OK again.
 +
 
 +
- We found again gas leakage with the three cells in about the same area as with the two cells. The amount of leakage was about the same (bubbling above 80-100 ccpm) as with the two cells, indicating that the problem is in the second cell. Bill suspects it is the seam on the wire frame between the PCBs that may have been somehow damaged during the installation. To fix the broken wire and look at the leakage place we decided to unstack the package down to the second wire frame. After finding the broken wire on the frame that is on the stringing table we decided to continue with this tomorrow.  
  
 
== Engineering ==
 
== Engineering ==
  
 
+
- Bill: the new fixture and hubs with adjustable height should be ready by the end of the month. Probably we will use them for the second package. The first fixture also can be refurbished to be used with the new hubs. Two more gusset rings ready tomorrow. Parts for the HV brackets and cooling system are also out for production. After the meeting: the package support brackets will be at JLab today. 
  
 
== Electronics ==
 
== Electronics ==
  
- Chris is in vacation; will work on the board that will bring the signals from the daughter cards outside for testing. While testing the resistors on the PCB's, Anatoly found that some percentage (~5-10%) of the resistors have lower values by 10-30%. These are current limiting resistor, but still Lubomir will discuss with Fernando if these need to be replaced.
+
- Anatoly tested several fresh PCBs: no broken resistors, but few resistors down to 50%. So, most likely the resistors were broken by us while making the frames, but the resistors with deviations from the nominal value came from the manufacturer. Fernando was surprised (before the meeting) and suggested replacing those that are more than 10% off, although these are current limiting resistors, i.e. not so critical.  
 
+
 
 
== Chamber testing at 126  ==
 
== Chamber testing at 126  ==
  

Revision as of 17:05, 22 September 2011

September 22, 2011 FDC meeting

Agenda

  1. Production Construction Tracking (Dave)
    • Status
    • First package tests (Lubomir)
  2. Engineering update (Bill)
  3. Electronics update (Chris)
  4. Chamber testing at EEL126 (Beni)
  5. Other: latest pictures of the package


Minutes

Participants: Eugene, Bill, Dave, Chris, Simon, Beni, Vladimir, Mark, and Lubomir. Vladimir is the new graduate student from MePhi Moscow.

Production

- Dave: started checking the continuity before taking the frame out of the stringing table: on the wire frame for cell#5 (that was just finished) one broken wire was found and was fixed today. Epoxy will cure overnight and tomorrow we will put on the stringing table the wire frame for cell#3 to fix one wire there too. Wire frame for cell#4 is ready, just needs final cleaning. On the last cathode (for the first package) the rigid-flexes were glued to the cathodes. Next, they will be tested with a generator and then the daughter cards glued.

- We discussed the reason for these broken wires, so far we had always one broken wire per plane. On the last one found on the frame for cell#5, we looked with a microscope. The wire was broken at the end of the epoxy right where it touches the soldering pad. The wire tip was bent at ~90 deg at this place somehow. It was not clear if the tip was inside or outside of the epoxy. The wire was checked by doing tension measurements on it. The only operation that happened later was cutting the wires and then doing the continuity measurements. One explanation could be a cold solder and then the wire brakes when twisting it. Dave suggested also that if the wire is above the PCB it may not be fully covered with epoxy and is easily breakable a that point.

- End of last week we put three cells in the package after replacing two wires in the second cell and changing all the O-rings. The first three cells were tested channel by channel by Vladimir. All were OK except no signal on one wire channel in the new third cell, most likely broken wire. The third cell was conditioned with HV relatively fast, but then suddenly developed very high current; we left it over the night at 1kV and then in the morning it was OK again.

- We found again gas leakage with the three cells in about the same area as with the two cells. The amount of leakage was about the same (bubbling above 80-100 ccpm) as with the two cells, indicating that the problem is in the second cell. Bill suspects it is the seam on the wire frame between the PCBs that may have been somehow damaged during the installation. To fix the broken wire and look at the leakage place we decided to unstack the package down to the second wire frame. After finding the broken wire on the frame that is on the stringing table we decided to continue with this tomorrow.

Engineering

- Bill: the new fixture and hubs with adjustable height should be ready by the end of the month. Probably we will use them for the second package. The first fixture also can be refurbished to be used with the new hubs. Two more gusset rings ready tomorrow. Parts for the HV brackets and cooling system are also out for production. After the meeting: the package support brackets will be at JLab today.

Electronics

- Anatoly tested several fresh PCBs: no broken resistors, but few resistors down to 50%. So, most likely the resistors were broken by us while making the frames, but the resistors with deviations from the nominal value came from the manufacturer. Fernando was surprised (before the meeting) and suggested replacing those that are more than 10% off, although these are current limiting resistors, i.e. not so critical.

Chamber testing at 126

- Beni started rearranging the space at 126. He swapped the electronics and the gas racks and added another rack with a second VXS crate. Now there's enough space around the racks.

Other

- For the Lehman review next month Eugene needs new results from the production chambers. Beni explained his results about the chamber efficiency for the second cell. Lubomir will also prepare some plots from the test of the second cell using fAD125. As for the first production package, the plan is to have it ready before the review but most likely by that time still there will be no results from the tests with the DAQ.

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